TT SHO PROJECT
New Member
cool thanks man.. ill grab teh denso'sSuperchargedSHOguy said:Denso IK20s for the plugs and motorcraft or taylor wires. The plugs are pricy, but they were highly recommended to me.
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cool thanks man.. ill grab teh denso'sSuperchargedSHOguy said:Denso IK20s for the plugs and motorcraft or taylor wires. The plugs are pricy, but they were highly recommended to me.
TT SHO PROJECT said:i dissagree with the knock statement i drove my stang around for about a year with teh wrong ecu running WAY lean.. it rattled and knocked all over the place when i boosted it... (honest human mistake) the pistons where stockers 155k miles.. came out looking like new no damage.. re ringed it and it was new again (blown head gasket from running lean) so i do know the sound of lean knock.. like marbles in a tin coffe can.sorry just thought id bring that up.
TT SHO PROJECT said:so im gonna first fix the harness and oil return line that keeps bursting!!! arrrrgggg.... gonna make a metal return line probably stainless if i can find some.
sho_sc said:5.0L have MUCH thicker #2 ring landings that stock SHO pistons, but you don't have to take my word on it.
ok i should of worded that better..... there is no restriction... it just like rubs up on something and it tares and starts to **** oil .. im just useing heater hose for the return line. im gonna Try to make a metal line for it so this will stop being a problem. oh yeah and i have the crank case fully vented so thats all goodOff Road SHO said:The RETURN line is bursting? What's it made of? Is something restricting it at the pan, mabe too small of a fitting or too much blow-by pressure?
You need to really vent the crankcase on your motor also. The Blow-by is tremendous on FI stock motors.
Tom
Tom
twr said:I know from first hand knowledge, that once you here knock on a FI SHO motor, you have already broken a piston. The hicup you described reminds of when PanamaPat's car broke 2 ring lands. Pulled nice and strong, then hicup and pulled strong again. Of course the blow by coming out of the oil cap was a dead give away too.
cheap? lol this is practicly free!!. i had all the main parts laying around just needed to buy the oil line/2 fittings and some heat wrap. now thats cheap!SHOblime said:You should change your name to "GHETTO TT SHO PROJECT"
it's all good though....I'm for doing it cheap as well!! don't worry about all the haters!!
TT SHO PROJECT said:i dissagree with the knock statement i drove my stang around for about a year with teh wrong ecu running WAY lean.. it rattled and knocked all over the place when i boosted it... (honest human mistake) the pistons where stockers 155k miles.. came out looking like new no damage.. re ringed it and it was new again (blown head gasket from running lean) so i do know the sound of lean knock.. like marbles in a tin coffe can.sorry just thought id bring that up.
TT SHO PROJECT said:heres a quick update... after ranking in some miles with it running mint it started to lose power again like it does in teh hickup just more of a steady loss not on and off.. and only boostin to 5psi if im lucky.... i burst a intake tube.. i used the stock tb to maf rubber elbow.. i guess it doesnt like boostburst a thumb size hole in it still makes boost tho, just dog rich.
its metered air that im leaking... so it runs mega rich... yeah i like driveing things to destructionsilversho89 said:Id figure itd be running lean with unmetered air entering the intake.
I still stand by my previous statement and think you should park it until you figure out these issues. But i guess if your putting a 3.2 in it, boost away at 5lbs till it doesnt run anymore.
Rob
yeah what you saidSaleen SHO said:its not sucking air into the intake any more... it is under pressure, Rob.
only at idle is when that might happen.
well im not Trying to **** this car i really want it to keep working...(but if it dies then its time for a 3.2) just for now i have no choice since i have no money to fix it. been looking for a job so i can do this thing the right way.. and the timeing shouldnt be pulled unless if thats what the sho ecu does on its own... but i dont know much about the sho's tuning so i dunno. this things got about 130k miles on it pretty sure with no 120k mile stuff done to it... so im playing with fire slapping a turbo on this car... but so far so good just working out lil bugs like the discharge tube bursting a thumb sized hole in it under boost hehe.SHO#7 said:I hate to see that you are going to try and break this car. But could the problem be that with higher boost, the WOT timing pull is more noticed. Like the car does not like that.
No boost here. Just reading along. If I sound way off, sorry.
Mike