High pitched whining from engine bay

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Johnbigdog

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If you have a pressure pump, you could always disconect the wastegate control valve and open up the wastegate, then go for a test drive to see if the noise is related to the turbocharger system.
 

SHO_Off420

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I think I will just try another test with my remote bluetooth microphone, get it near the turbo and listen.
The easiest way to test for boost leak is get a PVC plug that fits your intake right after your filter, thread a quick connect air fitting on it and hook up a compressor to your intakr, you can take it to 10 or 15 psi and listen for air leaks. I dont remember whether you've tested for boost leak yet, ive had a very busy week and haven't gotten to loon at mine yet hopefully I can get to it this Saturday and also get the 02 sensors replaced
 

SHO_Off420

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So this noise ended up just going away before I could troubleshoot it, I think it was a leak somewhere on th airbox as I had it removed for transmission work, i must have put it back in crooked or something.
 

rickshawSHO

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The easiest way to test for boost leak is get a PVC plug that fits your intake right after your filter, thread a quick connect air fitting on it and hook up a compressor to your intakr, you can take it to 10 or 15 psi and listen for air leaks. I don't remember whether you've tested for boost leak yet, ive had a very busy week and haven't gotten to loon at mine yet hopefully I can get to it this Saturday and also get the 02 sensors replaced
So tried this today. Had to fit plugs to clean air duct, throttle body connection, crank case vent. I used ****** for vent hose that runs to power brake booster to pressurize. Blew the plug out on clean air duct several times, had to clamp this real tight. Anyway, at 16 psi, could not hear any hissing. Have dealer appointment later in September. Let's see if they can figure it out.
 

Johnbigdog

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This may have been brought up already.. Did you inspect your recirculation valves? You won't find an internal leak with the above test.
 

rickshawSHO

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This may have been brought up already.. Did you inspect your recirculation valves? You won't find an internal leak with the above test.
I did inspect these valves initially when I removed the rear compressor outlet duct to check for splits. I removed both valves to check how these were seating and put 12v to the solenoid to check if they actuated. Best as I could tell everything was good. Doesn't mean one might be defective. Thanks for that suggestion.
 

rickshawSHO

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Well, I finally had the dealer diagnosis the issue as "failing turbo", although I'm not real convinced since I've been driving it for 6 months without any noticeable loss in performance. Makes 16psi boost, just it squeals! Anyway, rear or right bank turbo replacement.......$2800. So my initial investigation in Chiltons and crawling under and over the engine, yes, it will be a bitch. Chiltons, step #6, remove the front subframe. I can see this might be necessary but that's a lot of work. Saw one YouTube video of an Explorer the pulled the CV driveshaft instead. I'm going to watch that again, it may have been Ecoboost 4 cylinder, not V6. Otherwise, no other videos or Flex or Taurus SHO to help. Will search Forum to see if a member has shared any video or photos for DIY
 

Zpak

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Well, I finally had the dealer diagnosis the issue as "failing turbo", although I'm not real convinced since I've been driving it for 6 months without any noticeable loss in performance. Makes 16psi boost, just it squeals! Anyway, rear or right bank turbo replacement.......$2800. So my initial investigation in Chiltons and crawling under and over the engine, yes, it will be a bitch. Chiltons, step #6, remove the front subframe. I can see this might be necessary but that's a lot of work. Saw one YouTube video of an Explorer the pulled the CV driveshaft instead. I'm going to watch that again, it may have been Ecoboost 4 cylinder, not V6. Otherwise, no other videos or Flex or Taurus SHO to help. Will search Forum to see if a member has shared any video or photos for DIY
Hit up @802SHO
He came out of those trenches not too long ago. And yeah screw paying $2800. You can get a set of upgradded turbos for less. That’s two D’s for a double dose of pimpin.
 
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