Bluezone
Tailgaters will be prosecuted.
Matt had a look had several logs from dead stop to straight 3rd gear pulls. He says it looks like my Boost control valve is dirty. So it's sticking and not operating smoothly, oscillating waste gate operation to control boost. Headed down to Ford dealer tomorrow to order a new one.I had a similar experience, except mine gave me some numbers I was happy with, but then when he printed the numbers they were all completely different…….makes no sense and the printed numbers were lower…….I was so confused….I did 3 runs, two runs had damn near identical numbers, then I swapped to 1 psi less boost tune and ran a little less. Every time the dyno told us the numbers on a big *** screen…like a projector on the wall….it was exciting, I sat in the car with him, numbers would show up on the projector screen in front of us…with that correction(whatever it is for weather). Then happy and excited he goes to print the numbers as I’m ready to leave and all the numbers are different now. So idk what it really was….I don’t know if ANY of the numbers are legit. Then I backed into a random truck axle on the ground as the tech ghosted me and I took the car off the dyno myself which was weird as ****, bc after the first roller I hit my brakes but my car rolled forward again onto the other roller…..I would have preferred that he drove it on and off the dyno lol! The truck axle damaged my front chin spoiler, he didn’t charge me for that dyno session…..so I left with numbers that didn’t add up and damage to my car. I have no desire to jump back on a dyno anytime soon.
It said I was about 463hp and 569tq on a 19 psi tune and 418 and 522 on a 18 psi tune. Not much cool down between the 3 runs and I think the 18 psi tune was down so much bc after a flash my OAR is lower initially. Then printing the data said the 18 psi tune was 379hp and 406tq. I only took a pic of the results of the 18 psi tune on the dyno screen, but you can see on the graph where it is now only 379/406. So I have one of the fastest (underpowered) SHO’s around. This was a Mustang dyno and I honestly couldn’t make any sense of the numbers ……it was just a complete waste of time. And fixing the chin spoiler cost me $220….the dyno was $150 that he didn’t charge me bc if that axle on the ground. So meaningless numbers and I was out $70 plus my time. View attachment 82179View attachment 82180View attachment 82181View attachment 82182View attachment 82183View attachment 82184View attachment 82185View attachment 82186View attachment 82187







