avocadoman1
New Member
the bearing obviously was going out.
very loud whining.
when i took to test at Auto Zone, the thing heated up to hot to touch. although it tested out fine.
so i ordered a new one, took a day to get, noted the size of the pully as recommended here. it was an exact match with the same coding etched into it.
the removal and installation...all i can say is what a PITA.
thanks to all for old threads that spelled it out.
i did it without dropping the sub-frame as many have suggested.
the most difficult part was the upper bolt.
my hands (even with gloves) look like swiss cheese, and they're sore as all get out.
anywho...i took off the tie rod (as suggested), squeezed it thru the small opening.
now ready to rock and roll.
works great (knock on wood!) right now, and no whining sound anymore.
very loud whining.
when i took to test at Auto Zone, the thing heated up to hot to touch. although it tested out fine.
so i ordered a new one, took a day to get, noted the size of the pully as recommended here. it was an exact match with the same coding etched into it.
the removal and installation...all i can say is what a PITA.
thanks to all for old threads that spelled it out.
i did it without dropping the sub-frame as many have suggested.
the most difficult part was the upper bolt.
my hands (even with gloves) look like swiss cheese, and they're sore as all get out.
anywho...i took off the tie rod (as suggested), squeezed it thru the small opening.
now ready to rock and roll.
works great (knock on wood!) right now, and no whining sound anymore.
