Bull Geek
Member
It looks like Racer X was on to something. No signs of headgasket problems at all 
Finally fired the car up for the first time in months. Ran the engine for 30 min. 2500-3000 RPM, letting the cooling fan kick on each time. Car wouldn't overheat. Coolant reservoir was fine. No leaks of coolant anywhere. No head gasket problem found. The prior owner of this car was taken for. Too bad.
Engine issues found:
-Water pump tensioner is weak. Pump was not turning when car first turned on.
-Valve cover gasket leaks make a nice smoke show
-Oil filter adapter o-ring needs replacement
-IAC needs cleaning/replacement.
Next step is to pull the car into the garage, yank the valve cover off and check for welded camshafts.
The car lived in Commerce/Royston GA from 1997-2002. Maybe it got welded by FPS...James Short Ford serviced it during that time according to Carfax.
Finally fired the car up for the first time in months. Ran the engine for 30 min. 2500-3000 RPM, letting the cooling fan kick on each time. Car wouldn't overheat. Coolant reservoir was fine. No leaks of coolant anywhere. No head gasket problem found. The prior owner of this car was taken for. Too bad.
Engine issues found:
-Water pump tensioner is weak. Pump was not turning when car first turned on.
-Valve cover gasket leaks make a nice smoke show
-Oil filter adapter o-ring needs replacement
-IAC needs cleaning/replacement.
Next step is to pull the car into the garage, yank the valve cover off and check for welded camshafts.
The car lived in Commerce/Royston GA from 1997-2002. Maybe it got welded by FPS...James Short Ford serviced it during that time according to Carfax.